
This mine was being worked by Matthew Dore and Partners in 1739 but, by
1777, it had been acquired by Messrs Scott and Jeffries. In 1777, they
installed the first Boulton & Watt engine in this area, a 30" pumping
engine costing £800. The life of this engine was very short, however, as it was
sold to a nearby colliery in 1782. By 1789, the mine had been acquired by John
Weston & Co and they purchased a 45" engine from Boulton & Watt.
Its life was only a little longer than its predecessor, however, for in 1797 it
was sold to Alex McDonald and moved to a colliery at
The mine commenced work again in the early 19th century and a 70"
pumping engine was erected at Old Engine Shaft. The Shrewsbury Chronicle dated
February 1st 1838 gives an interesting account of the celebrations that took
place.
"On Friday last, Mr Cross of
About 1pm, this grand piece of machinery began to have fresh fuel added
to its boilers and for several moments the spectators were breathless with
anxiety till the beam lifted its majestic head and Mr Cross named her "The
Queen Victoria" amidst the tremendous cheering of a vast multitude, the
band playing "God Save The Queen".
The company retired to a large Booth where several hogsheads of most
excellent ale and large quantities of bread and cheese were distributed to the
workmen and multitude after which some hundreds footed it on the "light
fantastic toe", to Cambria's favourite instrument, the harp and two
violins, while members sat down to an excellent dinner in the office of the
company and adjoining rooms. After dinner, the usual loyal toasts were given
and drank with enthusiasm - "The Bog Mine Company and prosperity to their
undertaking" was next proposed and responded to with reiterated cheers
..."
When work ceased again in 1844, this shaft was stripped of its pitwork.
The company was in financial difficulties by 1859 and a petition for winding up
was made by a shareholder. He alleged that the manager, Mr Chenall, was fraudulently
converting shares to cash and that the company was in debt. At the same time,
however, a prospectus appeared in the Mining Journal in an attempt to rework
the mine on a larger scale.
In 1870, work on a large scale was again commenced and a 200 H.P. engine
with 70" cylinder was installed for pumping. The engine had a beam
weighing 26 tons and a 10ft stroke, working 16" plunger lift pumps which
were 120 yards long. The engine was named
In 1872, a letter by E.Cavendish Tahourdin appeared in the Mining
Journal. He stated that the water level had now fallen to the 100 fathom level
and, in a later letter, pointed out that it had cost £2,000 in the last 8
months to lower the water 26 fathoms. He forecast that, as the remaining
capital was only £2,000 and there was 59 fathoms yet to be pumped, the company
would be forced to make a further call on the shareholders or go out of
business. He also commented that the company only held the lease for 21 years
and 7 of these would be up before the shaft was bottomed. An official of the
company wrote and indignantly denied these facts but, before the year end, a
call was made on shareholders for more capital. By June of that year, the shaft
was nearly dry but reports in the Mining Journal show that the task had been
very difficult. The pumping costs had been greatly underestimated and the
company were in financial difficulties.
In 1874, the engine was recorded as working at 7 strokes per minute and
drawing 877,000 gallons per day. Later in the year, pumping from the bottom
levels, this became 41/2 strokes per minute and 563,800 gallons per day. The
shaft had finally been pumped dry but the expected bonanza was not forthcoming.
The 'old men' had filled the levels with deads and it was found that the tales
of rich veins were just not true! The company were forced to borrow capital and
mortgage the machinery to keep working and it was proposed to move the 70"
engine to Bunting's Shaft for winding, replacing it with a more powerful
pumping engine. If this had happened, it would have made the engine the largest
winder in the country but by 1875 the mine was in the hands of the liquidators.
At this late stage, the mine began to show better results but, despite optimistic
reports from Captain Harris, the company was wound up.
The mine was last worked on a large scale in 1883 when there was a small
output from above water level, as no pumping was being carried out. In 1897,
John Smitham of Tankerville commented on the bad state of the pumping engine,
boiler house roof and chimney. At this time, Captain Oldfield was making a last
attempt to start full scale work at the mine. Bunting's Shaft was later used to
pump up to the Boat Level, 52 fathoms below surface at this point, but no
details are known of the engine used. The shaft was finally used for winding
and a small horizontal winder was in use here until after the First World War,
when barytes were extracted. The wooden headgear was in situ until 1960 when it
was dismantled. At Ramsden's Shaft, sited at the other end of the Bog sett,
there was an electric winder which was probably the first to be used in
The site belongs to Shropshire County Council but little now remains at
the main site, despite its long and chequered history, and most of the tips
have been removed for roadstone. Both Main Shaft and Buntings Shaft have been
filled, although the headgear on Buntings Shaft was still standing in 1960. A
few foundations of the miners' institute have been preserved as the site of
some interpretation boards. The Somme Tunnel is still open for 135 yards, with
a metal grille at the entrance that is locked in winter to protect hibernating
bats. Next to this is the rectangular powder house that is in an excellent
state of preservation.
At SO360979 are the remains of the terminus of an aerial cableway which
carried barytes 5 miles for treatment at Minsterley. When the volume of mined
mineral decreased, this was replaced by a traction engine pulling carts. There is a collapsed shaft to the east of
this.

To the south is the capped Ramsden’s Shaft, sunk in 1915, which now lies
in a stable yard. The sites of Tews No.1 and No.2 Shafts are now covered by
trees and a search failed to find them. Either they have been missed in the
thick foliage or they were infilled when the trees were planted. Swag Shaft is
just in the trees by the side of the track leading to Nipstone Rock but has
been filled to the top with tree thinnings. It was descended in 1976 and,
contrary to a plan which shows a shaft and crosscut, was found to be an incline
shaft. The rock was blackened, perhaps by fire or explosion. A square
depression to the south on a large mound may be the Bog climbing shaft shown on
old plans.